The start of an eventful day stared at 06:40 with plenty of wind from the west and I was making fast progress although not always quite in the right direction as I adjusted course to make it more comfortable in the almost following and confused sea. At this stage I was aiming to cross the Merry Men of May, a very dangerous “Roost” or breaking tidal race that forms on the west going stream, just after the tide turned east and to go straight into Scarpa Flow.
A small group of whales, probably "minke", rather longer than the boat came alongside briefly but I was unable to get photos, the bubbles of one breathing out did get worryingly close at one point!
As the wind died mid-afternoon, I was using the engine and
made my waypoint 6 miles short of the Merry Men within a couple of minutes of
optimum. Then at about 17:00, 6 mile north of Scabster the engine stopped. A
quick investigation in a choppy sea showed that there was no fuel at the engine
but there was >= 20 litres of usable fuel (enough for almost 14 hours use) in the tank.
Clearly that was not going to be fixed quickly with the most likely cause being
the infamous “Diesel Bug” (a Bacteria that lives in oil, particularly if there
is water present, if forms a fibrous jelly that can block up the whole system.
Sancerre is an unlikely candidate having a bladder fuel tank and therefore
little or no condensation in it and having been regularly dosed with proprietary
treatments, but no one is completely immune if contaminated fuel, particularly with
white diesel including bio diesel, is loaded).
So, it was up with the sails and I started making slow
progress towards Scabster in Thurso Bay. Initially I made some progress but the
wind dropped to zero and I was being swept towards the race off of Dunnet Head
at about 1.5 knots and would likely end up in the Merry Men roust. Having given the coast guard a “heads up” as I set sail we
kept in touch until at 18:40 it became clear that the wind was unlikely to
return any time soon (it didn’t) and I issued a “Pan Pan” and was towed into
Scabster by the RNLI at about 19:30.
I found the problem almost immediately when I started to
clear the cockpit locker to turn off the fuel before checking the primary fuel
filter. The base of the locker rests on the hull outboard and a fairly narrow
(about 15mm) batten on the inboard side. I had reinforced the top of the
floorboards with a strong-back in case the boat inverted in a knock down and to
stop reserve fuel cans sliding about, but did not think to do anything under
the floor as it had been OK for 40 odd years.
Update: There may have been a different reason for the failure, when in 2021 I decided to replace the bladder fuel tank I was deliberately running the tank low to reduce the amount of fuel I was going to have to remove, in rough seas of Portland Bill the engine stopped from lack of fuel, I realised what was happening quickly stopped the engine, put more fuel in and after bleeding the engine was off again.Subsequent calculations showed that when I ran out I should have had at least 20 litres of usable fuel when I ran out and there was c 30 litres more always unusable in the 100 litre bladder (I always assumed a capacity of 50 litres per info that came with the boat) due to the position of the outlet and more particularly because a fold in the bottom of the bladder where it rested on the hull was holding fuel aft of the fold and away from the outlet. It is possible that the choppy sea off of Scabster and that fold was to blame rather than the slipped cockpit floor. Posts on how I replaced the fuel tank with one in stainless, the cockpit floor and the water tank can be found here.
Not knowing where I could next refuel I had put completely
full cans in pace at Port Ellen (usually I only put 15 litres in my two 20
Litre cans to make them easier to handle) and with a top up at Tobermory I had
75 litres weighing over 70 Kg on the floor. Then having had very rolling seas for
20 miles or so the floor shifted and with some damage slipped down and trapped
the flexible fuel line stopping fuel flowing.
Getting the fuel flowing again was then easy although bleeding
the engine was not as I found I could not get one of my spanners onto one of
the injectors, but in the end (about 21:00) the engine fired up again and I
then had an hour or so putting all of the removed woodwork back in place.
No comments:
Post a Comment