It was a bit of s struggle getting hoses on, even with lots of hot water, but I got there in the end.
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There is a "Y" junction bottom left leading to the seacock, the holding tank outlet pipe going behind the bowl, the direct outlet is waiting to be cut and connected to the diverter via the anti-syphon loop. The green pipe is for the automatic bilge pump |
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Getting the diverter straight and fixed to the panel was the biggest struggle mainly due to lack of room plus stiff pipes and pipe connections that would not rotate (with jubilee clips slack). |
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The finished job. The board left is a drop down table, rarely used now that I wear a beard so don't need it shaving using the mirror out of picture right. If I venture into the Baltic or some other areas I will have to put an eye on the panel to "lock" (probably with a cable tie) the diverter to feed to the tank as is required in places to prevent an accidental discharge. |
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The holding tank and filter fully plumbed in, the breather goes to the chain locker as there is insufficient freeboard to put it through the hull without a high risk of getting water in the filter. |
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The Henderson Mk 5 pump in position with the ball valve left. All plastic components are by Trudesign, the seacocks are genuine bronze (not DZR Brass) by "Blakes". The pump is capable of emptying the tank in less than 30 seconds. Lots of jubilee clips, doubled for all connections below the water line or hidden are needed for piece of mind and to keep surveyors and insurance companies happy. |
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The hatch, installed when I converted the forepeak to a wet area had to be butchered, I can still get my spare washboards in the locker but I'll have to find somewhere else for the spare tiller. For access I'll need to keep this area reasonably free of obstructions so things I might need quickly or regularly are going to live in the locker. |
All together it took about 3 days but I had the advantage of my work some years ago replacing the original vanity unit and installing panelling and the electric conversion to the toilet.
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Servicing the clean water input side of the unit, the output side was not as straightforward. |
As I was working in the area a deep service on the 5 year old macerator seemed to be a sensible idea, unfortunately it as not straightforward; two slot headed machine screws were unmovable, I ended up bringing it home, drilling off the heads, disassembling, bending the 650mm M5 machine screws through c 90 degrees and using the bend to get leverage to free them after applying lots of penetrating oil.
Fortunately nothing was damaged so it only cost a couple of bolts, lots of swearing, several hours and a "wasted" visit to the boat when I tried to do the service whilst on board.
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